Robot arm update #2

I’m in a trial and error phase when it comes to printing the largest components for the arm.

After a 15 hour print, i had to change the filament for one of them, and accidentally pushed the nozzle 2cm into the print and destroyed it.

The print quality on the other hand for the part was surprisingly good. This leads me to think that i can manage to print every part except two at home.

 

 

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